Maintenance Log May 2013


May 29, Wednesday, to June 7, Friday 2013


Went on a driving trip from Delcambre, to Atlanta to visit with our children. While in Atlanta, we drove to Tampa to visit family and to attend my sisters memorial service. We came back to Atlanta, spent more time with our children, then drove back to Delcambre.


May 28, 2013, Tuesday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.


Went to the shop, and put a second coat of Watco teak oil finish on the bottom of the cockpit hatch. Also dug out goodies and presents to take to Atlanta, loaded up the Black Beast. I checked all of the fluids in the Black Beast before going back to DREAM AWAY.


After breakfast, we welcomed two transient cruisers to the marina. Once we got them all settled in, Kitty took them into Abbeville for lunch at Shucks, and then took them shopping.


I did not join them. I had other fun projects to occupy my time! I cleaned out the manifold (Sea Chest), the main input strainer, and the individual strainers for the air conditioner, the ice maker, the refrigerator, and the aft air conditioner. When I put it all back together, I connect the dock hose to the hose for the air conditioner, the ice maker, the refrigerator, and the aft air conditioner, and run high pressure water through the hoses to clean them out.


As the summer comes on, I will be doing this task every three weeks.


Manifold (Sea Chest) and Main Input Strainer On Dock


Basket From Main Strainer


Refrigerator Strainer Taken Apart For Cleaning


Connecting Hoses To Manifold (Sea Chest)


May 27, 2013, Monday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee. Spent a couple of extra hours working on email, and updating the Google Maintenance Log, and the Google OpenROV log.


After we had a very nice breakfast, Stacy and I started the process of checking out the newly purchased Pepwave Surf SOHO 3G/4G Router w/ WiFi as WAN. Let me give a little background on the WiFi system presently used on DREAM AWAY. The present system is talked about in great detail in the Electronics & Navigation section of the DREAM AWAY web page.


The system works great, but the management of the EnGenius EOC1650 Bridge was a pain. Some of it my fault because of the location EnGenius EOC1650 Bridge. Each time you moved DREAM AWAY, and wanted to search for a new WiFi network, it was necessary to take my computer, with a CAT5 Ethernet cable, into the middle cabin. I had to clear access to the cabinet that had the EnGenius EOC1650 Bridge in it. I then disconnected the CAT5 Ethernet cable going to the Dovado UMR USB Mobile Broadband Router from the EnGenius EOC1650 Bridge, and connected my computer to the EnGenius EOC1650 Bridge via my CAT5 Ethernet cable.


Now I could manage the EnGenius EOC1650 Bridge. Once I got the bridge set up, I disconnected my computer from the EnGenius EOC1650 Bridge, and reconnected the Dovado UMR USB Mobile Broadband Router. Once the system came up, I could see if it actually worked by connecting to the Dovado UMR USB Mobile Broadband Router via the WiFi on my computer. If I was not able to access the Internet, I had to go back and do it all over again! Not a great management scenario.


Hopefully the new Pepwave Surf with the WiFi as wan would solve the present management issues. I have a Hyperlink 1 watt WiFi amplifier that is cabled to the EnGenius EOC1650 Bridge. I purchased a new cable to run from the Hyperlink 1 watt WiFi amplifier to the new Pepwave Surf SOHO 3G/4G Router w/ WiFi as WAN.


EnGenius EOC1650 Bridge Installed In Mid-Cabin


Hyperlink 1 Watt WiFi Amplifier In Garage


We connected one end of the new cable to the Hyperlink 1 watt WiFi amplifier, and the other end of the cable to the new Pepwave Surf SOHO 3G/4G Router w/ WiFi as WAN. We powered on the new Pepwave router, accessed it via WiFI, and did the management of it with no problems. It was a dream! We took everything down, and put the system back the way it was. As soon as I get some time I will run the new cable and get the Pepwave Surf SOHO 3G/4G Router w/ WiFi as WAN installed and running.


We then cleaned up, took showers, then had to deliver Stacy to the airport. He Caught his flight back home to Atlanta, and we drove back to DREAM AWAY.


When I arrived back on DREAM AWAY, I started in on the replacement of the Heart Freedom 25 Inverter/Charger. I brought the repaired unit to DREAM AWAY, and started the process. To change out the Heart Freedom 25 Inverter/Charger, it was necessary to remove the forward tool box in the garage.


Forward Tool Box To Be Removed


Once the tool box was removed off of the work bench, I had access to the Heart Freedom 25 Inverter/Charger that was screwed down to the bulkhead between the garage (Starboard SIde) and the main cabin. I removed the spare unit and placed it on the main cabin floor.


Spare Heart Freedom 25 Inverter/Charger On Main Cabin Floor


Now I installed the repaired Heart Freedom 25 Inverter/Charger unit. Because the Heart Freedom 25 Inverter/Charger is heavy, 60 pounds, it was necessary to block it up.


Blocked Up Heart Freedom 25 Inverter/charger


With the unit blocked up, I was able to screw it to the bulkhead, and complete the installation.


Heart Freedom 25 Inverter/Charger Installation Complete


I applied power to the Heart Freedom 25 Inverter/Charger, and the unit checked out perfectly. Tekris Power Electronics did a great job on the repair.


Now I will get the spare unit sent out to Tekris Power Electronics, and see why the status of the Heart Freedom 25 Inverter/Charger is not shown properly on the LINK 2000-R.


May 26, 2013, Sunday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.


Went over to the shop, and the first thing I did was to apply the first coat of Watco teak oil finish on the underside of the cockpit hatch. When I completed the application, I put the cockpit hatch and the two screens outside in the sunlight to expedite the drying process.


The day before I left on the trip to Tampa, I had loaned the tender to a friend on a boat here in the marina. She needed the tender to work on her boat. I took all of the gear, including the fuel tank over to the shop. I cleaned up the fuel tank, as it was pretty nasty. I also took apart the apparatus I have to display the running lights on the tender. This apparatus is fabricated from teak, and I am planning to sand it all down, apply the Smith’s penetrating epoxy, and then apply the Watco teak oil finish.


I also did the repair job on the Port Of Delcambre’s tent. The tent had two bent legs


I then went back over to DREAM AWAY, after putting the screens and the cockpit hatch back into the shop. Stacy, Kitty and I had breakfast, and then Stacy and I went back to the shop. We spent the remainder of the day working on the assembly of the OpenROV kit.


To follow along with the assembly, please look in the OpenROV section of the DREAM AWAY web page.


May 25, 2013, Saturday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee. Spent a couple of extra hours working on the web page and answering email while waiting for the crew to arise.


Stacy and I had breakfast, then went over to the shop. We spent the remainder of the day working on the assembly of the OpenROV kit.


To follow along with the assembly, please look in the OpenROV section of the DREAM AWAY web page.


May 24, 2013, Friday


Flew back from Tampa to Lafayette. Kitty picked me up at the airport, and we went back to DREAM AWAY. I got settled in, then went over to the shop.


Unpacked boxes, and verified we had all parts and accessories to start on the assembly of the OpenROV kit tomorrow.


OpenROV Kit And Accessories


Stacy will be flying in later today, so tomorrow morning, all I have to do is gather up all of the necessary tools and we are ready to go with the assembly of the OpenROV kit.


Next, I unboxed the Heart Freedom 25 Inverter/Charger that had arrived from Tekris Power Electronics the day I flew out to Tampa. I knew I would not have time to install the Inverter/Charger today, but I wanted to verify the unit arrived with no physical damage.


Heart Freedom 25 Inverter/Charger Out Of Box


Hopefully, I will get this repaired Heart Freedom 25 Inverter/Charger installed this weekend so I can get the spare unit sent to Tekris Power Electronics early next week.


I then applied a second coat of Watco teak oil finish to the top of the cockpit hatch and the companionway screens.


Cockpit Hatch With Second Coat Applied


First Screen With Second Coat Applied


Second Screen With Second Coat Applied


I then left the shop, and went back to DREAM AWAY. I took the cable with me I had ordered with the new Pepwave Surf SOHO 3G/4G Router w/ WiFi as WAN. I wanted to verify it would fit on my WiFi amplifier, and it did! This weekend Stacy and I plan to install and fully check out the Pepwave Router. If this unit works the way it is advertised to work, it will save me some significant WiFi bridge management issues. Kitty and I then took showers, and headed back to the airport in Lafayette to pick up our son, Stacy.


May 16, 2013, Thursday Thru May 24, 2013, Friday


Flew to Tampa on the 16th so I could visit with my sister over the weekend. As it turned out my sister was very sick. My sister passed away early in the morning on May 20th. I stayed over to help family with the transition.


I flew back to Louisiana on the 24th. Kitty and I will be going to Tampa the weekend of June 1st for the memorial service being held at the New Beginnings Christian Church.



May 16, 2013, Thursday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.


Went over to the shop to get some work done before I had to fly to Tampa. My sister is very sick, so I am flying to Tampa so I can see her this coming weekend.


I sanded the two screens, went over them with the tack rag, then applied the first coat of Watco Teak Oil Finish to the screens. The Watco Teak Oil Finish also works on mahogany, that is why I am applying it to the mahogany screens.


Watco Teak Oil Finish Applied To Screen


Watco Teak Oil Finish Applied To Screen


I applied the second coat of Watco Teak Oil Finish to the top of the cockpit hatch.


Watco Teak Oil Finish Applied To Cockpit Hatch


I then applied the second coat of paint to the wooden boat hook.


Second Coat On Boat Hook



May 15, 2013, Wednesday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.


Went over to the shop with my butt connectors, and tools, so I was able to wrap up the modifications to the eBay unit. The connectors were used to wire in the blower motor.


eBay Unit With Wiring Complete


Now I will have to wire the unit to the shop electricity, and bring one of the spare air conditioning cooling water pumps over to the shop. When I get the pump wired to the system, I will be able to test the system, and see if the money and effort were worth it!


I sanded off the rough spots on the top of the cockpit hatch, and wiped it all down with the tack rag. I then applied the first coat of Watco teak oil finish to the top of the cockpit hatch.


Cockpit Hatch With Coat Of Watco Teak Oil Finish


Went back to DREAM AWAY, and had breakfast.


I started in again on troubleshooting the wind instrument not functioning properly. On May 11th I had tested the wind display, and it worked fine. Now I wanted to test from the mast base junction box to the display. At the base of the main mast where all of the wires from the lights, radio and wind instrument come through the deck there is a junction box.


I opened the junction box, and disconnected the wind instrument wires coming from the masthead anemometer.


Opened Junction Box


I then connected my spare anemometer, base and wire to the input of the junction box.


Spare Anemometer, Base And Wire


When I powered up the instruments, the wind display functioned normally. Good news and bad news. The good news is, from the junction box at the base of the main mast to the wind display, everything works fine.


The bad news is the problem is the anemometer, or base that is at the top of the mast, or the wire leading from the base down to the junction box.


By the time I got everything put away, it was late. When I get some spare time, and Kitty can help me, I will got to the top of the main mast and remove the anemometer from the base and plug in the spare. Hopefully that will fix the problem. If it does not, I will have to replace the base and the wire in the mast.


May 14, 2013, Tuesday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.


Went over to the shop and continued work on the screens. I blew them off with air, then wiped them down with a tack rag. I mixed up a batch of Smith’s penetrating epoxy and applied it to the screens. I also applied another heavy coat to the wooden boat hook.


Smith’s Penetrating Epoxy On The Screens


Smith’s Penetrating Epoxy On The Boat Hook


Went to DREAM AWAY for breakfast. Before going back to shop I applied the fifth coat of Cetol to the main mast step.


Mixed up another batch of epoxy mash mix, and applied it to the bottom of the cockpit hatch.


Finally got all of the letters screwed down to the name boards. Now the name boards are officially finished.


Completed Name Boards


Completed Name Boards


Back in March I had talked about the Cruisair Air Conditioner I had purchased off of eBay, and how it arrived in Delcambre. I will not go into all of the back and forth between us, UPS, and Staples. Lets just say, through the efforts of Kitty on the phone, we got our settlement.


My original Cruisair Air Conditioner, of 18 years, had failed, and I replaced it with the new model Dometic Stowaway series reverse cycle air conditioner. I knew that my old Cruisair Air Conditioner had a leaking evaporator, but everything else worked. When a used Cruisair Air Conditioner came up on eBay at a very inexpensive price, I decided to purchase the one off of eBay. When I got the unit from eBay I would use it as a spare after a checkout. I would cannibalize parts off of the failed unit, and be covered for air temperature control for the foreseeable future.


Good plan, and it will mostly work out that way. The fly in the ointment is the unit I purchased from eBay came in damaged. Now I have to take some parts off of the failed unit to get the unit from eBay working. Naturally the failed unit and the unit from eBay are not exactly the same, so I have to make a couple of adjustments to make everything function.


The plastic housing on the blower assembly on the eBay unit, had been broken off of the evaporator. I had to remove the blower assembly from the failed unit, and install it on the eBay unit. Because of differences in the electrical connection between the control electronics and the actual air conditioner, I also had to change the electronics and the control unit.


I got all of the changes made on the eBay unit, except for two electrical connections. I did not have the butt connectors or the tools with me, so that will be finished tomorrow.


eBay Unit During Modifications


Failed Unit During Modifications


eBay Unit After Modifications


Failed Unit After Modifications


May 13, 2013, Monday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.


Went over to the shop and completed the sanding and scraping of the screens. They are ready for the application of the epoxy.


Sanded Screen


Went back to DREAM AWAY, and verified the propane connection for the Hummer Grill at the propane tank. It seems if I do not really tighten the connection, the propane leaks out. I will have to replace the original POL valve with the newer QCC valve.


I had finished off the large acrylic insert for the companion way several days ago, but did not put in the before and after photos of the improvement.


Large Acrylic Insert, Before Modification


Large Acrylic Insert, After Modification


May 12, 2013, Sunday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee. Worked on web page and maintenance log until Kitty awoke.


Spent Mother’s Day with Kitty, and did not work on DREAM AWAY.


May 11, 2013, Saturday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.


Went over to the shop and mixed up a batch of Smith’s penetrating epoxy and applied it to the bottom of the cockpit hatch. I also applied a good soaking to the bottom of the wooden boat hook.


Cockpit Hatch With Epoxy Applied


Wooden Boat Hook End Soaked In Epoxy


Continued working on the companionway screens. I had decided to scrape all of the varnish off of the screens, rather than do a couple of maintenance coats. When the screens were down to bare wood, I planned to apply the Smith’s penetrating epoxy to them, and then apply the Watco teak oil finish. Hopefully this combination will be easier to maintain.


Sanding Screens


Continued to get the letters on the name boards. Not as easy as it might seem. The letters were all individually drilled to put the screws in them, so trying to get the correct letter lined up in the correct position was proving more difficult than expected! Most letters I only had two choices, but the “A” I had six to choose from!


Letters On Name Boards


Went back to DREAM AWAY and had breakfast. After breakfast, I re-installed the instruments back into the cluster under the main boom gallows.


Before putting putting the instruments in their proper position, I made sure all of the connecting wires had the proper connectors on them. I had previously purchased connectors for just that purpose, as I did have to replace several connectors.
I also wanted to check out my wind instrument. It had not been working correctly. I wanted to see if the actual instrument was bad, or the wiring on the anemometer at the top of the main mast. I had a spare masthead anemometer and the wiring, so I could connect the spare directly to the instrument while the instruments were not in the pod.


The wind Instrument functioned normally connected to the spare masthead anemometer, so the actual instrument was not the problem. I would have to do some more troubleshooting. In the meantime, I put all of the instruments back into the pod.


Instrument Pod And Wiring


Checking Instrument Connections


Instruments Back Into The Pod



May 10, 2013, Friday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee. The rain was amazing, so stayed on DREAM AWAY and worked on the web page.


Went over to the shop in the late afternoon, after the rain had stopped, and the floods had receded. Did some more welding on the tubing I will be using for the main cabin grab rail. Trying to do some fill on some of the bad welds. Trying to get back into the swing of welding, and it is a slow process.


Did some more work on the nameboards. I am putting all of the original green letters back on the nameboards. They will look really good when I am finally finished.


Got the hole cut in the panel the cockpit instruments are in. Like everything else, cutting the hole was easy, getting everything set up on the drill press and clamped down, took all of the time.


Drill Press Setup To Cut Hole


Hole Cut In The Panel


All Instruments Back Into Panel


May 9, 2013, Thursday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.


Today was not a DREAM AWAY maintenance day. We went to our Doctor in Delcambre to start the examinations for our annual physical.


We then drove to Abbeville to do our laundry, and also stoped by Lowe’s, and purchased some of the required items for the OpenROV project coming up at the end of the month.


While at Lowe’s I also purchased at extension cord, so I can continue with the installation of the second WiFi router at the North Pier Marina. The installation did not go well, as the second router seems to be DOA.


May 8, 2013, Wednesday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee. Worked on web page and email, until it was time to leave for Dermatologist appointment.


When we returned from the appointment at the dermatologist, I changed into my work clothes, and went to work on deck.


The area under the jerry jugs on the deck of DREAM AWAY, had never been cleaned up properly, so I got out the brushes, toilet bowl cleaner and elbow grease. I got the area on both the port and starboard sides all cleaned up, and looking good.


Had a bit of excitement at the marina before I went back to the shop.
Kittie, off of one of the cruising boats at the marina had been stung by a wasp, and she is highly allergic. Lots of emergency medical folks came, but the bottom line was, she was taken by helicopter to Iberia Medical center because of the wasp sting bite. The good news is she was released after only being at the Iberia Medical center for about three hours.


I had finally decided to install a new Raymarine ST-60+ compass in my instrument cluster in the cockpit. I had purchased the compass in April of 2012 to replace the Autohelm ST-50 compass. It was the last of the original ST-50 system which I had purchased in 1995. The compass still worked, but I wanted to get the newer one installed.


I disconnected all the instruments and removed the instrument cluster. I then took the instrument cluster and went over to the shop. Before going over to the shop I dug out the proper size hole saw to cut the instrument cluster.


When I got over to the shop I removed all of the instruments from the teak wood panel. I was preparing the panel to have the hole enlarged for the new Raymarine ST-60+ compass.


Instruments And Panel On Work Bench


I mixed up a batch of the epoxy mash mix, and used it to install the filler piece of plywood on the underside of the cockpit hatch. This is being used to fill in where the rotten wood was cut out of the hatch


Plywood Installed In Cockpit Hatch


I applied the third coat of Watco Teak Oil Finish to large acrylic insert.


May 7, 2013, Tuesday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.


Went over to the shop, and mixed up another batch of the Smith’s penetrating epoxy and applied it to the cockpit hatch. I then put the cockpit hatch out in the sun to get the epoxy to “kick off”


Epoxy On Cockpit Hatch


Next Item was to do a complete inventory of the OpenROV kit. This activity is completely covered on the OpenROV section on the DREAM AWAY web page.


I mixed up a second batch of the Smith’s penetrating epoxy and applied it to the cockpit hatch. I then loaded the Cutco knife holder in the Black Beast, and went back to DREAM AWAY for breakfast.


I did the install of the Cutco knife holder in the galley, and we were able to install the two new knives we purchased at the boat show in March. We had ordered the Traditional Cheese Knife and the Petite Santoku knife to add to our collection. That is why the Cutco knife holder had to be modified.


Cutco Knife Holder Installed In The Galley


After breakfast, I applied the fourth coat of Cetol to the main mast step. Then I went over to the Shrimp Festival grounds, and helped lay out the grid for the Delcambre Seafood and Farmers Market on May 11th.


When I finished the laying out of the grid, I went back to the shop and mixed up a third batch of the Smith’s penetrating epoxy and applied it to the cockpit hatch.


I took my high speed grinder over to the shop and worked on the stainless steel tubing I am going to use for the main cabin hand hold.


Sanding On Stainless Steel Tubing


Last Item for the day was the varnish. I applied the seventh coat on the nameboards. I applied the second coat of Watco Teak Oil Finish to large acrylic insert.


May 6, 2013, Monday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee. Worked on computer getting caught up with email and working on the Maintenance Log


brought over finished the teak wire cover, and all of the Panduit wire duct covers, and installed on DREAM AWAY.; applied expoxy to top of cockpit hatch; welded on tubing; Helped get transients, Connie and Wayne off the dock and on their way.


Went over to the shop, and on the way I picked up a 12 VDC battery that was still good, but Kittie was getting rid of. They had upgraded all of the batteries on their boat, and some of the old batteries were still good. I needed a battery for the starter I was installing on the Yamaha outboard for the dinghy.


When I got to the shop, I pulled out the electric start kit I had purchased for Kitty, so she would be able to start the Yamaha. I used the newly acquired battery, and tested the the starter. It worked perfectly! Now all I have to do is get the electric start kit installed on the outboard, and get a battery box installed in the dinghy.


Did a bit more welding on the tubing for the main cabin hand hold. Working on getting my steady hand back, and the setup for the welder.


Welded Tubing


Went over to DREAM AWAY for breakfast. Took over the teak wire cover, and all of the Panduit wire duct covers.


Teak Wire Cover, And Panduit Wire Duct Covers


I installed the Panduit wire duct covers in the main cabin and the forward cabin.


Panduit Wire Duct Cover In Front Cabin


Now I had to install the teak wire cover in the mid-cabin. This cover was covering all of the wires going to the electronic shelf, mid-cabin fan and forward cabin reading lamp. Before installation could be completed, I had to remove the printer from the top of the electronic shelf.


When the printer was removed, I had to move some wires around to make sure I had enough slack wire to make the angles in the teak wire cover.


Mid-cabin Wires Exposed


Last Item for the day was the varnish. I applied the sixth coat on the nameboards. I applied the fifth coat of varnish on the Cutco knife holder. I applied the first coat of Watco Teak Oil Finish to large acrylic insert.


May 5, 2013, Sunday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee. Worked on computer getting caught up with email and working on the Maintenance Log


Chris at Tekris Power Electronics asked me to put a paper inside the box with the Heart Freedom 25 Inverter/Charger that had the return shipping information, and an explanation of the problems with the unit. I printed out this information, and an address label. I then went over to the shop.


When I got to the shop, I got out several pieces of scrap foam. I cut and fit the pieces of foam to completely wrap the Heart Freedom 25 Inverter/Charger in.


Foam Around Heart Freedom 25 Inverter/Charger


Once I got the foam all around the Inverter/Charger, I put the information sheet inside, then closed up and the taped the box. I put the address label on and it was ready to go. I shipped it out in the afternoon via the USPS.


Heart Freedom 25 Inverter/Charger Ready To Go


Next was the cockpit hatch. The Smith’s penetrating epoxy I applied yesterday had set up very hard, so it was time to epoxy the piece of plywood into the hole in the hatch.


Hole In The Hatch


I sanded and scraped out the hole, so that it was smooth and the piece of plywood fit perfectly. I did a dry fit of the piece of plywood, then I mixed up a batch of mash mix. The mash mix is a mixture of the epoxy and the Cabosil ormicroballoons. It is about the consistency of peanut butter. I used the mash mix to put the plywood into the hole in the cockpit hatch.


Ready For Hatch Repair


After the repair was made I placed three weights on the piece of plywood to insure it would set up properly.


Weights On Cockpit Hatch


Last Item for the day was the varnish. I applied the fifth coat on the nameboards, the teak wire cover, and all of the Panduit wire duct covers. I applied the fourth coat of varnish on theCutco knife holder.


May 4, 2013, Saturday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee. Alan and I filled our go cups with coffee, and headed to the shop.


When we got to the shop we started in. Yesterday I decided to use the newest parts to build my main engine. That meant I would use the new long shaft lower housing I had purchased off of eBay on the main engine. This meant I had to move the whale tail from the old lower drive to the new lower drive.




While Alan started on the whale tail project, I looked around the shop for a suitable platform to attach the Heart Freedom 25 Inverter/Charger, and make it ready for shipment. I was able to find a piece of plywood already attached to some 2 X 4’s, that is perfect to mount the Heart Freedom 25 Inverter/Charger. I also put two pieces of foam insulation between the Inverter/Charger and the plywood to act as a cushion.


Wooden Pallet For Heart Freedom 25 Inverter/Charger


I got some help from Alan, and we cut up a cardboard box, and stapled it to the pallet to form a box around the Heart Freedom 25 Inverter/Charger. When that was finished, Alan and I got back changing the whales tail to the new lower drive.


We measured and looked, and then measured again. While I was drilling holes in the lower drive for the whales tail, Alan was cleaning out the threads in the zincs. There are six bolts total holding the whales tail to the lower drive. Two of the bolts have nuts on the end. The other four bolts are bolted into the zincs. We scraped the paint off of the area on the lower drive where the zincs are bolted to make sure we have good contact. While we were working on thelower drive, we also took the water pump apart and checked the impeller, which was good.


Fitting Whales Tail To Lower Drive


Whales Tail Bolted On


We then sanded down the all of the exposed teak wood on the cockpit hatch, and sanded down and smoothed the filler that was applied yesterday.


I mixed up a batch of the Smith’s penetrating epoxy and applied it to the hatch and really soaked in the wood around the cut out. This took some time, as I would pour the epoxy in the hole, let it soak through, and kept it up until no more epoxy would soak in.


Cockpit Hatch Showing Epoxy Soaked In


Cockpit Hatch With Epoxy Applied


May 3, 2013, Friday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee. Alan and I filled our go cups with coffee and headed over to the shop.


We started in on the main outboard engine, to replace the bracket assembly. As with most projects of this type, there is a lot of parts that have to be removed from the engine before you can actually change the bracket assembly.


Preparing To Remove Power Head Bolts From Bottom Cowling


Basically the engine has to come completely apart. When we separated the power head from the bottom cowling, we discovered the oil seal housing for the drive shaft, was eaten away, and would need to be replaced.



My storage room neighbor, Huey, came to his storage area, and I asked him about getting the cream hardener. He said I should try V & V Auto Parts in Delcambre. I called them and they did sell the needed cream hardener.


We then went back to DREAM AWAY to have our breakfast. We left DREAM AWAY, and stopped by V & V Auto Parts. I purchased the cream hardener, and went back to the shop.


Alan continued on with the disassembly process of the outboard engine. I mixed up a batch of the Dyna-Glass filler with the cream hardener, and applied it to the cut out rotten area in the cockpit hatch.


Cockpit Hatch With Filler Applied


As we waited for the filler to harden, I joined Alan in the continuing disassembly process. I wanted to get the old bracket assembly off of the engine, so I could figure out how many new parts I would need to put the main engine and spare engine back together. The spare engine was already apart, and I knew what I needed there.


Removing Old Bracket Assembly From Upper Casing


Old Bracket Assembly Being Replaced



Engine Parts Removed



We were able to make a list of the items necessary for the reassembly of both engines. Looking at all of the parts I had acquired for both engines, I decided I would take all of the newest and best parts, and marry them with my main power head, and build the main engine. I had the power head rebuilt in 2010 in Guatemala. I would use all of the older parts to build the spare engine.


Parts Ordered For Both Outboard Engines


Last Item for the day at the shop was the varnish. I applied the fourth coat on the nameboards, the teak wire cover, and all of the Panduit wire duct covers. I applied the third coat of varnish on the Cutco knife holder.


I had talked earlier in the week to Chris at Tekris Power Electronics discussing the issues I was having with my two Heart Freedom 25 Inverter/Chargers. When Alan and I went back to DREAM AWAY, I got out my spareLINK 2000-R voltage monitor, and connecting wire. We used the wire to attach the LINK 2000-R voltage monitor to the currently installed Heart Freedom 25 Inverter/Charger. I got the same indications, or lack thereof, so I decided I do have some kind of signal problem with the Heart Freedom 25 Inverter/Charger.


The otherHeart Freedom 25 Inverter/Charger was popping its internal circuit breaker, so I decided to send that unit to Tekris Power Electronics for repair first. I dug the Inverter/Charger from under the forward cabin birth, and hauled it out to the Black Beast.


Tomorrow, Alan and I would build a shipping crate for the Heart Freedom 25 Inverter/Charger.


May 2, 2013, Thursday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee. Alan and I got a cup of coffee in our go cups and went over to the shop


Worked more on the cockpit hatch, sanding and scraping. I need to get all of the old Cetol off of the hatch, as I plan to apply the Watco Teak Oil Finish to the hatch. This will be done after the rotten area is repaired, and the whole hatch is soaked in the Smith’s penetrating epoxy.


I have the polyester filler I need for the hatch, but all of my cream hardener is very old and not useable. We drove over to Leblanc Oil, and Touchard’s Marine looking for the cream hardener, but were not successful. Will probably have to drive into Abbeville to find it.


We then went to work on the spare Yamaha outboard power head. I still do not have the broken off bolts removed. I had ordered and received a Neiko screw extractor set. It contained five sizes of left hand drill bits, and five easy outs. We drilled the holes and used the easy out, but we still did not get the broken off bolts out of the power head. It looks like to save this power head, I am going to have to take it to a shop that specializes in removing broken bolts. I am sure I am going to end up using a Helicoil.


Bottom Of Power Head With Broken Bolts


Since we were making no progress with the spare engine, Alan and I decided to go to work on the main Yamaha outboard. I had purchased a used bracket assembly off of Ebay, to replace the bracket assembly presently on the engine. The bracket assembly was in pretty bad shape, but needed replacement.


We started in on the project, but a new cruising boat was coming into the marina. I applied the third coat of varnish on the nameboards, the teak wire cover, and all of the Panduit wire duct covers. I applied the second coat of varnish on the Cutco knife holder.


Alan and I closed up the shop and headed over to the marina, to help the newcomers dock. When we finished with the docking process, and had some social time, it was time to quit for the day.


May 1, 2013, Wednesday


Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.


Went over to the shop and started in on doing an inventory of all of the items that arrived in the OpenROV kit. I still did not have the printed inventory with me, but I wanted to make sure all of the parts in the kit arrived in excellent physical shape. Everything seemed to be in order, and I even got all of the parts back into the original box! You can keep up with the kit assembly and testing on the DREAM AWAY web page with this link.


The epoxy had set up on the Cutco knife holder, so I sanded it all down it preparation to apply thr first coat of varnish this afternoon.


Sanded Cutco knife holder


Next I started on the cockpit hatch. The timing on this project, turned out to be great. Yesterday on our anniversary, Kitty gave me a new tool. It is a Rockwell Sonicrafter Oscillating Tool, and it is the perfect tool to cut out the rotten wood in the cockpit hatch.


Installing Blade On New Tool


I measured off a square section around the rotten wood on the underside of the hatch, then used the new tool to make the cuts. It worked perfectly. This is going to be a nice tool to use in situations just like this.


Tool Laying Near Rotten Area In Hatch


Cut Out Area In Bottom Of Hatch


I then cut out a square of ⅜” mahogany plywood to fit into the cutout of the hatch. I trimmed and sanded the plywood piece until it fit into square. Now it was ready to be epoxied into place.


Cut Piece Of Plywood Fit Into Cut Out Squart


I took the Shakespeare SeaWatch 2025 TV antennas apart, and checked all of the connections. I also took the small printed circuit boards out of each antenna, and the control box looking for broken or damaged wires or electronic parts. Needless to say I could find nothing amiss, so I am afraid we are out of luck with the attempts to get the Shakespeare SeaWatch 2025 functioning.


I started on another project today, that will not need to be completed until we do a long passage again. I have been requested by several of our crew to put some handrails near the center of the main cabin. This is an excellent idea as there really is nothing to grab onto between the companion way handholds, and the handholds at the forward end of the main cabin. Just a lot of empty space.


Grab Rails At Companionway


Grab Rails At Forward End Of Main Cabin


I am welding some pieces of 1” stainless steel tubing together to make part of the new handrails. When they are complete, they will have mounting plates at each end, and will be thru-bolted to the deck.


Welded Tubing


Last Item for the day was the varnish. I applied the second coat on the nameboards, the teak wire cover, and all of the Panduit wire duct covers. I applied the first coat of varnish on the Cutco knife holder.