Maintenance Log June 2013

June 30, Sunday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

The tender was still in the water after working with PERELANDRA, so I put the engine back on the lifelines, and the tender back onto the davits.

I washed the mainsheet in a mild soap and bleach solution to remove built up dirt and mildew. Rinsed it off and then hung it out to dry. Continued scrubbing the cockpit sheet nets. They are slow to get clean. May have to resort to the laundromat.

Worked on the computer to get caught up on email and scanning in receipts and documents.

Welcomed Transients To The Marina

Went and took a shower, then drove to New Orleans to Get Kitty after her trip to see friend Kathy. Got back to DREAM AWAY around midnight!

June 29, Saturday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went over to the shop and repaired the screen from one of the main cabin hatches. The screen I repaired yesterday was larger than the main cabin hatch, so I was able to use the old screen to repair the screen for the main cabin hatch.

Repaired Main Cabin Hatch Screen

I checked out the window air conditioner I have and verified it worked properly. Mark and Kittie are having issues with their on board air conditioner. Before I offered them the window unit, I wanted to make sure it worked.

I sanded the V-Berth insert, and the Panduit wiring duct covers. I masked the V-Berth insert in preparation for the application of varnish.

I applied the first coat ofSmith’s penetrating epoxy on the shelf for under the stove in the galley, the batten for the front of the shelf, and the two supports for the shelf.

Smith’s Penetrating Epoxy Applied To Shelf And Parts

Went back to DREAM AWAY, and removed the wood deck in the anchor area of the bow pulpit. Fit the fiberglass grating, but still needed some trimming for the perfect fit. Marked the grating for cutting.

Deck From Anchor Area On Bow Pulpit

Back into spring cleaning mode. I cleaned the main cabin, including both lockers on either side of the settee shelves.

Went back to the shop and cut the fiberglass grating to the adjusted measurements.

Fiberglass Grating After Adjustments

I nailed the batten onto the front of the shelf to be put under the stove in the galley. The batten is to keep pans from sliding off of the shelf.

I applied the second coat of varnish to the Panduit wiring duct covers, and the first coat of varnish to the V-Berth insert.

Varnish Applied To Panduit Wiring Duct Covers And V-Berth Insert

I applied the second coat of Smith’s penetrating epoxy to the shelf and supports for under the galley stove.

Went back to DREAM AWAY, and fitted the fiberglass grating to the deck of the anchor area on the bow pulpit. It is a perfect fit.

Fiberglass Grating On Bow Pulpit

All that remains is to purchase J-bolts to secure the grating to the bow pulpit.

June 28, Friday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went over to the shop and repaired the screen for the aft cabin. Had to cut new screen material, and insert the screen into the frame.

Frame With New Screen Material

I brought over two butt connectors, so I connected the blower on the spare air conditioner to the power controls. I powered up the unit, and everything functioned normally. Now all I need is a small piece of hose, and I can check the system out with the cooling water running through the system.

I applied the dye to the Panduit wiring duct covers. When they dry they will be ready for varnish.

Dyed Panduit Wiring Duct Covers

I cut the wood for the shelf I am putting under the stove in the galley. I also cut the fiberglass grating to be used on the bow pulpit anchor area.

Before leaving the shop, I took a couple of pictures of Mark’s diesel engine that is in the shop along with a bunch of parts he ghad stripped from the engine.

Engine From The Back

Engine From The Front

Parts Removed From Engine

Went over to DREAM AWAY, and fitted the shelf under the stove in the galley.

Went back into spring cleaning mode. I cleaned the pot and pan storage area under the microwave in the galley. Took the doors from the aft cabin, and the door from the main cabin to the mid cabin out on deck and washed and rinsed them.

I then cleaned the head and the storage area under the head sink. When that was finished the doors on deck were dry, so I put them back in their respective door jams!

I went back over to the shop and applied the first coat of varnish to the Panduit wiring duct covers.

It was then back to DREAM AWAY for a shower and adult beverages!

June 27, Thursday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Mark and I drove into Abbeville to get parts and wood for Mark and his engine project. The plywood and 4X4’s Mark purchased was to support the engine hoist in the main cabin of PERELANDRA, and to spread the load of the weight of the engine. Returned to the marina, dropped off Mark and his wood, and I went over to the shop.

I removed the old power and electronic controls from the spare air conditioner, and reinstalled the original power and electronic controls. I also got the pump connected all but one hose, which I will get later.

Long story here, but I could just cut off a short piece of the ¾” hose I have. My plan though, is to use that long piece of ¾” hose to run from the raw water washdown pump on DREAM AWAY to the raw water outlet on deck at the bow. I already have a hose run, but it has been cut into for fittings that are not needed now. That piece I want to remove from DREAM AWAY, and I will use that short piece for the air conditioner test.

I got all of the electrics and electronics connected except for the blower motor. I did not have two butt connectors. I powered it on and the unit started to cool. With no water to cool the unit, I shut it off, as I did not want to cause another problem.

Spare Air Conditioner Connected Up

Knew I was going to be using the tender today to move PERELANDRA to and from the shrimp dock, so I cleaned out the fuel filter on the tender fuel tank.

Fuel Filter Before Cleaning

Cut the teak wood tape for the two Panduit wiring duct covers I brought over to the shop yesterday. I then used the iron, and ironed the teak wood tape onto the Panduit wiring duct covers.

Teak Wood Tape Cut For The Panduit Wiring Duct Covers

Teak Wood Tape Applied On The Panduit Wiring Duct Covers

Loaded Troys wood into the Black Beast, then went back to the marina. I put Troys wood out in the sun on DREAM AWAY.

I then went into spring cleaning mode and finished cleaning under the galley sink and the galley stove. While under the galley sink, I also exercised the seacocks located there.

Under The Galley Sink

I took measurements for a shelf in the area under the galley stove. We need a shelf there to keep some of the large pans and the waffle iron from sliding down the hull every time you remove something in front.

The remainder of the day was spent helping Mark get the engine out of his boat. I was deeply involved, so was not able to take any pictures.

We used the tender as a tug, and moved PERELANDRA to the public dock in Delcambre. Mark had arranged to have Mike From Leblanc Oil come to the dock with his forklift. Mike drove the end of the attachment on the forklift into the main cabin of PERELANDRA. We attached the engine (short block) to a shackle on the fork lift. Mike very carefully lifted the engine, and the backed it out of the main cabin on PERELANDRA.

When the engine was on the dock, Mike walked back to Leblanc Oil. ark drove the forklift over to the shop, and we put the engine in the back entrance to the shop. Mark drove the forklift back to Leblanc Oil, and the came back to PERELANDRA. We used the tender again and got PERELANDRA from the public dock back to her slip on Pier “C” at the marina.

Mark cleaned up the inside of PERELANDRA to get it back to a live aboard boat again. His work was cut out for him. Good for him that I had the shop available for him to use to rebuild his engine.

June 26, Wednesday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went to shop with my digital DVM. Measured the input AC, and it seems good. Something must be different in the controls from the failed AC to the controls from the spare AC. Will have to do the exchange of all of the electrical controls.

Sanded the teak board I epoxied to use to cover the holes in the aft cabin. Needed to mix another batch of epoxy but the can of hardener was empty. I have a new can of hardener, but I could not get the pump out of the old can to put in the new can. I ended up destroying the old pump, so will have to purchase a new pump before I can mix any more epoxy.

Took most of Troy’s wood over to DREAM AWAY to sit out in the sun. This will accelerate the drying process.

Took eight doors from the aft cabin, galley and head outside on deck and washed them down with soap, water and high pressure water. Left them out in the sun to dry.

Performed the spring cleaning on the aft cabin. Removed two Panduit wiring duct covers to take to the shop, and glue on the teak tape.

Got on the computer and finally caught up on emails!

June 25, Tuesday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went to the shop, and got to work on the spare air conditioner. Got the blower connected, and applied power to the unit, but it would not power up! Very disappointing. I was hoping the controls out of the failed unit would work on the newer unit. I will have to bring over my digital VOM to verify the power.

Worked on the epoxied teak I will be using to cover the davit holes in the aft cabin. Mixed up a batch of epoxy and filled in any gaps in the teak that I had missed yesterday.

Teak Piece To Cover Davit Hole In Aft Cabin

I applied another of Watco teak treatment to the backside of Troy’s wood.

Went back to DREAM AWAY to work on the fresh water pump. The pump in the system was leaking, so I had to install one of the spare pumps. I carry two spare fresh water pumps, so I am pretty covered!

Freshwater Pump Removed From System

Leaking Pump Removed From System

Spare Freshwater Pump Installed Into System

Spent the remainder of the day spring cleaning the galley.

June 24, Monday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went to the shop and applied another coat of Watco teak oil finish to the back side of Troy’s wood.

Watco Teak Oil Finish Applied To Troy’s Wood

Started fabrication of a piece of wood to use to cover the holes left by the davit installation in the aft cabin. I am using several pieces of teak wood that was removed from the deck of DREAM AWAY many years ago. I lay all of the pieces on a flat surface, apply mixed epoxy to all the edges, and then clamp them all together.

Teak Wood Strips Clamped And Epoxied Together

Worked on getting all the necessary connectors on the water pump and the spare air conditioner so it can be tested properly.

Water Pump And Spare Air Conditioner

Went back to DREAM AWAY, took a shower. Kitty was packed, so we loaded up and I drove her to New Orleans so she could catch a flight to go visit friend Kathy. I returned back to DREAM AWAY arriving well after dark.

June 23, Sunday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee. Alan left this morning to go back home to Houston.

Went over to the shop and added more tension on the puller attached to the flywheel of the spare yamaha. Smacked the puller with a hammer, and the flywheel came off! I removed the flywheel and the magneto under the flywheel. Now I had the power head ready to go the machine shop.

I put the first and second coat of Watco teak oil finish on back side of Troy’s wood.

Worked on old air conditioner to remove parts off of the drip pan. Getting the drip pan ready to send to Stacy’s friend to fabricate a new drip pan out of stainless steel for the spare air conditioner.

Took outboard off of tender and put on DREAM AWAY. Pulled tender out of water and washed down the exterior and bottom of the tender. Also cleaned up all of the stainless steel rails and fittings on the exterior. When finished, I put the tender back on the davits.

June 22, Saturday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went over to shop and checked the puller on the flywheel of the spare outboard engine, it had not come loose. We applied some more Aero Kroil, tightened the bolts a bit more, and tapped the puller with a hammer. The flywheel remained fixed. We then set the power head aside. A few times during the day we would tap the puller with a hammer, and tighten up the bolts from the puller to the flywheel. When we left at the end of the day, the flywheel remained fixed.

We then started in on the main outboard engine. As mentioned yesterday, we had an almost complete engine. All that remained was putting the lower drive on the engine, which we did.

I also took pictures of the new serial numbers, and engine type since I used parts from a 9.9 HP outboard. It is still a 15 HP, it will be listed as a 9.9 HP.

New Serial Numbers And Engine Model And Year

The model I created with all of the new parts is:
15 ELG
15 = horsepower
E = Electric Start
L = 20"
G = 1988

The parts I used for most of the upgrades is:
9.9 MLHP
9.9 = horsepower
M = Manual Tilt Manual Start
L = 20" (Long Shaft)
H = Tiller
P = 1991

Complete Engine Ready For Use

We loaded the complete engine with the battery and the fuel tank into the Black Beast and went back to DREAM AWAY. We lowered the tender into the water from the davits, and then put the “new” long shaft 15 HP motor on the back of the tender.

We put the battery into the tender and connected it to the motor. We also connected the fuel tank that had very fresh gas in it with no alcohol in it. I tried to start the engine manually and with the electric start, but no go! Then I remembered I did not have the dead-man switch activated. I attached the dead man switch, and the engine started right up with the electric start. I also tried the manual start and that worked also.

It was so great to finally have the long shaft motor running. I had been saving parts off of eBay for over two years to get this accomplished. That was the good news. The bad news is there is no water running out of the Pee tube. This means the water pump is not working.

I decided rather than try to take the motor apart on the dock, we off loaded the motor from the tender and took the motor back to the shop in the Black Beast.

We took the lower drive off the motor. That is when I discovered I had not aligned the water tube coming out of the water pump up to the power head. We put the lower drive back on the motor being very careful to get the proper alignment of the water tube.

We took the motor back to DREAM AWAY, put the motor on the tender and started it up. We had water pumping out of the Pee tube! What a relief. Alan and I took the tender down the channel and when we were past the docked the shrimp boats, I opened it up. Right up on a plane with both Alan and I in the boat.

We went back to DREAM AWAY and got Kitty in the tender. Did the same trip again, and when the tender got up on a plane there was some cavitating. I adjusted the angle of the motor in relation to the transom of the tender. Went down for another ride, and it was almost perfect. I finally can get the tender up on a plane with three people in the tender.

We took the tender back to DREAM AWAY, and locked it to the dock. We took showers and had an adult beverage in celebration.

June 21, Friday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Alan and I had our coffee, and then went over to the shop to get started on the outboard engines again. We put together the puller with the proper bolts and bolted it to the flywheel on the spare engine.

As noted previously, I was trying to strip all of the parts off of the spare power head which included the flywheel and the magneto under the flywheel. I also had to remove the flywheel off of the main outboard so I could install the electric start kit I had purchased for Kitty. For the electric starter to function, I had to install a new flywheel.

We put the puller on the flywheel of the spare engine, and attempted to pop off the flywheel. We used muscle, a small hammer and liberal application of Aero Kroil. It was not going to work, as hard as we tried.

Well we went to plan “B”. We removed the puller from the spare flywheel, and attached it to the main flywheel. We applied some Aero Kroil, and then tightened down on the puller. After a few minutes of applying pressure, the flywheel popped off!

Old Flywheel With Puller Attached Beside New Electric Start Flywheel

Main Power Head with Flywheel Removed

We now knew the puller actually worked as designed. We put the puller back on the spare engine flywheel, and tightened up the puller as much as we thought reasonable. We applied some Aero Kroil, and then set the power head aside. A few times during the day we would tap the puller with a hammer, and tighten up the bolts from the puller to the flywheel

Now we could get serious about putting the main outboard engine back together, starting with the power head back. We installed the new flywheel and the starter. We also installed the manual start mechanism just in case!

Power Head With Starter Installed

When the power head was complete, it had to be mated with the bottom cowling. We did all of this using never seize with all of the bolts. We also had to clean the bolts, and some of the parts as we went along.

Power Head and Bottom Cowling Together

I already had the upper casing and the bracket assembly together, but we had to attach the tiller control to the bracket assembly. This turned out to be a lot more trouble that we thought. Getting everything lined up was interesting but we finally got it.

Alan Working On Tiller Control

When we finished with the tiller control, we were able to attach the upper casing and the bracket assembly to the bottom cowling. We almost had a complete engine. We were done for the day, so back to DREAM AWAY for showers and adult beverages.

June 20, Thursday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Alan and I went to the shop and worked on the two outboard engines. While Alan and I were getting all of the parts for each engine straightened out, we started putting the main outboard back together. Kitty went and purchased the required bolts to use my puller on the outboard flywheels, and also a tube of never seize.

I wiped down all of Troy’s wood, and put them outside in the sun to dry. I applied a coat of Watco on the cockpit hatch, and also put it outside to dry.

Wood Parts Outside To Dry

Wood Parts Outside To Dry

When Kitty came back to the shop with the bolts and never seize, Alan and I had to regroup! I decided I wanted to apply never seize to all of the bolts on the parts we had already put together on the main outboard. So now we took apart the bracket assembly and put it all back together with never seize.

Bracket Assembly And Upper Casing Back Together

June 19, Wednesday, 2013

Alan and I got up, had coffee, and hit the road, with a breakfast stop at a Whataburger.

We drove up to Porter, Texas, to Diamond Composite Structures. The man running the company, Vince Pena, remembered me from previous purchases. I purchased some pieces of the ¾” plate fiberglass for the hard dodger, and the main mast step. I also purchased fiberglass grating to replace the teak wood on the anchor area and the seat in the bow pulpit.

I asked vince about fiberglass rod of very small size that I am thing about using for security on the hatches on DREAM AWAY. He had a pile of carbon fiber tubes that he had used for arrows. I felt this would be perfect, because of the strength. He just gave me about 20 of the tubes!

We got all of the fiberglass parts loaded in Alan’s little FIAT 500, and

drove back to Delcambre. When we got to Delcambre we unloaded his car and headed to DREAM AWAY.

June 18, Tuesday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

The folks off of the cruising boat that came in from Texas this past Saturday, Sammy and Dick, were heading back to League City today. My friend Alan was coming over from League City to visit for a couple of days, and I needed some structural fiberglass from Diamond Composite Structures.

I made arrangements with Sammy and Dick to ride over to League City with them. I made arrangements with Alan to spend the night with him, and then on Wednesday drive up to Diamond Composite Structures in Porter, Texas, on our way to Delcambre.

The plan worked! Sammy and Dick dropped me off at the West Marine in League City, and Alan picked me up there. We went to Alan’s apartment, and I worked on his two computers to get them back up and functional. Alan and I had dinner and a couple of adult beverages, and hit the sack.

June 17, Monday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went over to the shop and worked on Troy’s wood. Not all of the Watco teak oil finish had dried sufficiently. I wiped down and sanded the pieces, and applied a third coat of Watco teak oil finish.

Had to run errands in Abbeville, so I took my spare Yamaha power head along to stop at an outboard shop. We stopped at a shop in Erath, and the owner told me he did not drill out and install helicoils. I would have to take the power head to a machine shop. He recommended a shop in Abbeville.

We finished up our shopping errands, and then went to the machine shop. I told to one of the technicians there, and he told me he could do the job, but I would have to strip all of the parts off of the power head. Now I had another project.

We went back to Delcambre, and I went to the shop to strip all of the parts off of the power head. I took many photos, so hopefully when the time comes, I will be able to get all of the parts back on the power head.

Power Head Before Parts Removal

I got all of the parts stripped from the power head except the flywheel. Of course I did not have the required bolts for my puller. As it turned out I needed 2 ½” long 5 mm metric bolts.

I got the new tube of BoatLIFE LifeSeal, and I finished applying it to the cockpit hatch.

Went back to DREAM AWAY to look for the required bolts, but of course did not have them.

I did call Boats.net, and talked to a person in the parts department. The o-ring I needed was listed as obsolete, but they had 15 in stock. I order three of them. One for my main outboard, one for the spare outboard, and of course a spare just to have!

June 16, Sunday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Spent a lazy day on fathers day. Worked on the computer trying to catch up, and spent time just reading. Kitty and I talked over our future plans, and pretty much decided to not stick to a hard a fast date to leave Delcambre. When I feel comfortable with DREAM AWAY, we will continue our cruise.

Since it was Fathers Day, Kitty asked me what I would like for a treat. I told her I would like her very good rum cake. She made me a rum cake, and we both enjoyed snacking on it and for dessert!

Finished Rum Cake

Pouring On The Rum Sauce

June 15, Saturday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went over to the shop and wiped down all of Troy’s mahogany pieces, and applied the third coat of Watco teak oil finish.

Started to work on getting the outboard motor back together. I had all of the parts to build a stock long shaft motor. When I went to put the oil seal housing (use link to my own pdf file) back on the engine, I realized I did not have an o-ring that was required. I then went through all of the parts and gaskets on hand to verify I did have all of the necessary parts, except one!

Later in the day, when I went back to DREAM AWAY, I looked on my parts list and got the necessary part number. I then went on the Internet, to Boats.net, and discovered the part number is obsolete. This will take more investigation!

Bottom Of Motor Where Oil Seal Housing Attaches

Original And New Oil Seal Housing

Went back over to the marina to welcome two cruising boats into Delcambre. One boat was from Texas, and the other boat was from Franklin, Louisiana.

Texas Cruisers Welcomed Into North Pier Marina

Louisiana Cruisers Welcomed Into North Pier Marina

June 14, Friday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went over to the shop and started in on Troy’s wood. Did the final sanding on all of the pieces. Arranged all of the pieces so that I could get to them and apply the Watco teak oil finish. I wiped all of the pieces down with a tack rag, and then applied the first and second coat of the Watco teak oil finish.

Watco Teak Oil Finish Applied To Troy’s Wood

Watco Teak Oil Finish Applied To Troy’s Wood

I received the Heart Freedom 25 Inverter/charger back from Tekris Power Electronics. They said they ran the unit over a weekend and it functioned perfectly? I hope so, but I now have my spare Heart Freedom 25 Inverter/charger back on the boat.

June 13, Thursday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went over to the shop and spent a couple of hours working on Troys wood. He had two fishing pole hangers that really took a lot of time to sand out. Lots of holes and curves!

Applied the BoatLIFE LifeSeal to the masked off cockpit hatch. Could not do the complete hatch because the tube of BoatLIFE LifeSeal had hardened at the bottom of the tube. Was able to return the tube for a new one, but it delayed the completion of that part of the project.

Cockpit Hatch Waiting For More BoatLIFE LifeSeal

Went back to the Marina, and welcomed another cruiser to the dock.

New Cruiser Tied Up To Pier C

June 12, Wednesday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went to shop, and straightened up all of the stuff we brought back from Atlanta, and some other stuff I had acquired. Had to put it all away and out of the way, to get the shop back into full production.

Finished masking out the cockpit hatch, so it is ready for the application of BoatLIFE LifeSeal.

Went back to DREAM AWAY, to have breakfast. After breakfast, I defrosted the freezer, and cleaned up the condiment trays in the refrigerator.

Ice Scraped Off Of Freezer Holding Plates In Freezer

Ice On Expansion Valves

Ice Removed From Expansion Valves

When I finished cleaning up from the defrosting project, went back to shop and started sanding on Troys wood for his boat, and the teak pieces for the navigation lights on the tender.

Troy’s Pieces Sanded And Ready For Watco Application

Went back to DREAM AWAY and welcomed two transient boats to North Pier Marina. When we got the two boats all settled in and properly welcomed, I went to work on the second router at the North Pier Marina.

Welcome Transient Boaters

Welcome Transient Boaters

June 11, Tuesday 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went to shop started masking top of cockpit hatch. Have to get the hatch masked off so I can apply the BoatLIFE LifeSeal between the teak boards on top of the hatch

Hatch Partially Masked Off

Our largest yacht at North Pier Marina, PENDANA, left today. We waved off Chris and Sarah as they headed to Florida. The M/Y PENDANA will remain in Florida, while they commute back and forth to Jeanerette, Louisiana, where they have their boat company, Metal Shark Boats.

Chris And Sarah On PENDANA

PENDANA Leaving the Marina

I worked on marina landscaping, weeding the gardens for about 30 minutes. The remainder of the day was spent working on web page other computer activities.

Kitty and I attended the monthly Port meeting that evening starting at 1800.

June 10, Monday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went over to the shop and masked off the bottom of the cockpit hatch and the V-Berth insert for the forward cabin. Did the preparatory sanding, and the the wiping down with the tack rag. I mixed up a batch of the two part white paint from Guatemala, and applied a coat to the cockpit hatch and the V-Berth insert.

Masked V-Berth Hatch

Painted V-Berth Insert

Masked Cockpit Hatch

Painted Cockpit Hatch

The remainder of the day was spent taking Kitty to the doctors and the hospital for a test, that did not work out as planned. On the way back from Lafayette, we stopped and shopped for groceries.

June 9, Sunday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Spent the remainder of the day working on the computer to catch up on email, maintenance logs, and scanning in papers.

Kittie and Mark, on PERELANDRA, left to start their trek to Florida.

PERELANDRA Leaving North Pier Marina

That was the good news for them, and we will miss them. The bad news is they were back that afternoon with a blown engine! They had proceeded about 20 miles down the GIWW, when the engine froze up! An initial diagnosis was that the number six cylinder had overheated and froze. They had to be towed back to North Pier Marina. Needless to say they are very down and disappointed. This will be an ongoing issue.

June 8, Saturday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went over to the shop and unloaded the Black Beast. We had brought some material and tools from Atlanta to help with the ongoing projects on DREAM AWAY. I also brought back some stuff that I am going to sell on eBay. I have been meaning to do this for a long time but never got to it.

Sanded on bottom of cockpit hatch to get it ready for paint. Also sanded on the V-Berth filler brought back from Atlanta, and the tender navigation light holder. The light holder really needed attention.

Sanding On Cockpit Hatch

Sanded V-Berth Filler

One other group of parts I brought from Atlanta was my exhaust elbow for the main engine. When I had to replace the exhaust elbow several years ago, I purchased all of the parts to have a spare (Overkill!!). When we left Texas in 2009, I did not take the spare with me. It is four years later, so I decided it would be a good idea to have the spare with me.

I verified all of the parts fit together and looked like it should when fitted to the engine. I am considering welding the whole fitting together or keeping the parts separate. If the parts are separate, they are much easier to store, but then a far amount work ro put it together with hi-temp pipe dope. If I weld the whole thing together, it is a bear to find space for, but can be put in place with little effort. The jury is still out.

Exhaust Elbow In Vice

Went back to DREAM AWAY, and dressed ship. I put out all of normal flags, but added the International Code Flags. Today was National Marina Day, and we are having a big party to celebrate.

DREAM AWAY Dressed Ship

May 29, Wednesday, to June 7, Friday 2013

Went on a driving trip from Delcambre, to Atlanta to visit with our children. While in Atlanta, we drove to Tampa to visit family and to attend my sisters memorial service. We came back to Atlanta, spent more time with our children, then drove back to Delcambre.

While in Atlanta I had shipped off my second, spare, Heart Freedom 25 inverter/charger to Tekris Power Electronics. This unit worked just fine, but the status of the Heart Freedom 25 inverter/charger is not shown properly on the LINK 2000-R. I re-used the shipping box that Tekris Power Electronics sent the first Heart Freedom 25 inverter/charger back to me.

Recording Serial And Model Number Before Shipment