Maintenance Log July 2013

July 31, Wednesday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, and checking the weather, while making a pot of coffee.

Spent extra time getting information for Kitty printed, and trying to get some air conditioner information. Also working on the Maintenance Log for June and July.

The technician from Tim’s air conditioning called and said he was on a call, but would come to DREAM AWAY as soon as he finished. He came, and to make a long story short, I had fixed the problem but did not know it. Yesterday when I cleaned out all of the strainers, and blew out the hoses with the pressurized dock water, there must have been a minor blockage in the AC cooling hose. After cleaning out the hose yesterday, I did not attempt re-starting the air conditioner, because I was afraid of damaging the unit.

When the technician ran the unit, it did not cool properly, because i did not bleed the air out of the cooling lines yesterday. Today after we bled the air out of the AC cooling lines the system ran with no problem, and has been the remainder of the day.

Next on the agenda, I went out to pier C in our tender, and cleaned all of the plants that were growing on the dock. Not a big item, but it did not give a good professional appearance. When that was completed, I mowed the grass at the marina, and did a lot of grass trimming, and garden weeding. That pretty much ended the day.

I still have to find the switch numbers to properly repair the aft air conditioner.

July 30, Tuesday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, and checking the weather, while making a pot of coffee.

Also spent some time working on the Internet getting in touch with the folks from whom we purchased the new Dometic ECD16K-HV air conditioner last January.

The bottom line after spending a lot of time on the Internet and the phone, is I am screwed and did not get a kiss! The Dometic support person said it sounds like the problem is either water flow or the high pressure switch. I know it is not the water flow, so it must be the high pressure switch. The support person said those switches rarely fail that new, the usually fail in the five year range.

I also found out the warranty for this unit is one year if purchased and installed by a Dometic certified technician. If purchased from anyone else and self installed the warranty is six months from date of manufacture! To put more salt in the wounds, I can not find the manuals that came with the unit. So I am trying to find an electronic copy of the manuals.

The aft air conditioner works, but the off/on switch is not working. I removed the air conditioner controls from the panel, and used butt connectors to wire out the switch. I verified the aft air conditioner worked, then shut it off.

Aft Air Conditioner Control Panel

To insure there were no water flow problems with either air conditioner, I cleaned out the main strainer for the manifold (Sea Chest), and the manifold (Sea Chest). Also cleaned out the strainers for the ice maker cooling pump, the refrigeration cooling pump and the forward and aft air conditioner cooling pumps. During this cleaning process, I also cleaned out the hoses for all of the cooling pumps using high pressure water from the dock.

When I finished and cleaned up from this process, I started the aft air conditioner. Kitty was out doing laundry, and I wanted the aft cabin cool when she returned. A problem presented itself with the aft air conditioner. When it had run for about 10-15 minutes, the breaker on the control panel would pop. Not a good thing. I would wait about 3 minutes, reset the breaker, and it would run again for about 10-15 minutes.

So now I have an additional problem with the aft air conditioner. I suspect it is a problem with another switch on the control panel. The input wire (black), is has been very hot and is corroded, and the connector on the switch is not very nice either. I will try and get the numbers off of the switch and see if I can find a new one.

I also contacted Tim’s air conditioning in Broussard, Louisiana, to see if they could come out and repair the high pressure switch on the forward air conditioner. The Dometic support person recommended Tim’s air conditioning as the closest Dometic approved repair vendor. The technician was gone for the day, but the secretary said the technician would call first thing tomorrow morning.

I then went over to the shop and got the awnings for DREAM AWAY. They are not in the best of shape, but will probably help keep the inside temperature down until they fail. I put up the aft awning and the midships awnings. They are in the best shape, but they need to be replaced. That project has moved up the list a lot. The forward awning is in such bad shape, I did not put it up. I will probably put it up tomorrow, and leave it up until it blows out completely.

July 29, Monday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, and checking the weather, while making a pot of coffee.

The MacBook Pro is still up and running, with no apparent problems, so I will continue to catch up on my email, and trying to get the June and July Maintenance Logs updated.

Drove into Lafayette for doctors appointment for Kitty. Doctor was delayed by two hours, so we did not get back until 1830. When we arrived on DREAM AWAY, the forward air conditioner was down.

We were getting a HPF error indication which is a high pressure shutdown. This error usually indicates a cooling water flow problem. It did not appear to be the problem, but I cleaned out the main input strainer, and the specific air conditioner strainer. I also vacuumed the air filter on the evaporator. Nothing helped the problem.

We went to bed without air conditioning. It was not bad at all, the temperature was in the mid 70’s, and we have plenty of fans.

July 28, Sunday, 2013

Started off the morning with my normal ritual of getting on the Internet and checking the weather, while making a pot of coffee. Having computer problems, so no checking of email.

I had left a permissions fix program running on the MacBook Pro all night long, and it did not finish. I then decided to do a backup from my Time Machine backup hard drive on the MacBook Pro. Somehow I completely screwed that up! It was a bust!

As of this point in time I am backing up from my last clone which is two months old! I do have a backup of all my data files from yesterday morning, and email, so I will be able to restore those files if the backup is successful.

I have been successful, and I am now back up and running on the MacBook Pro. I have been able to download email, so the remainder of today will be getting caught up on email, and working on the maintenance logs for both June and July.

While Kitty was shopping yesterday she had purchased two Energizer “C” NIMH batteries. I installed one of them in the Nicro day/night vent, and that fixed the problem with that unit. Now I truely have Nicro day/night vent!

An unusual occurrence on the Delcambre Canal this afternoon. After my shower I was enjoying an adult beverage in the cockpit, and a spud barge and towboat came by, and went up into the lake.

Towboat With Spud Barge

Towboat Pushing Spud Barge

July 27, Saturday, 2013

Started off the morning with my normal ritual of getting on the Internet and checking the weather, while making a pot of coffee. Having computer problems, so no checking of email.

Went over to the shop, and did some cleanup because Mark has moved some of his stuff out of the shop. He still has a bunch of engine parts in the shop, but they will be going on his newly installed engine on PERELANDRA.

I unpacked the new Evolution Rage III compound miter saw, and put it together and tested it. Looks like it will be a dandy. I was able to cut my stainless steel square tubing at a 20 degree angle. This saw will be most helpful with future projects.

Evolution Rage III Compound Miter Saw In Box

Evolution Rage III Compound Miter Saw Ready For Use

Evolution Rage III Compound Miter Saw After Cutting Stainless Steel Square Tubing

I then applied the fourth coat of varnish on teak pieces to cover the davit holes in aft cabin, the teak piece to cover the winch hole in the main cabin, and the teak electrical wire cover.

Left the shop and then back to DREAM AWAY to try and get out of the hole with my computer problems. The MacBook Pro I am using is dying a slow death. I did all of the backups, and have moved all of my data to my backup Gateway PC. In fact I am doing this entry from the Gateway. I have to try and get the MacBook Pro back up and running from the backups I have been doing.

I got the power washer out to see if I could make any progress on the rust stains on the outside of the hull. No effect whatsoever. I will have to remove the stains the old fashioned way, with elbow grease, and stainless steel cleaner. A good toilet bowl cleaner works wonders on stainless steel and stained fiberglass.

July 26, Friday, 2013

Started off the morning with my normal ritual of getting on the Internet, and checking the weather, while making a pot of coffee. No email because I am having some computer problems.

Today was the big day for Mark and PERELANDRA. Will not go into a huge amount of detail, but Mark had been working for the past week on rebuilding the diesel engine for his trawler. Today was the day we put the rebuilt short block back into the boat.

Lots of work and effort, but we got PERELANDRA moved, the engine inserted in the main cabin, and PERELANDRA moved back to her dock. Because of several issues, we did not get the engine mated up to the transmission. To be continued tomorrow.

Engine Lifting Device In PERELANDRA’s Main Cabin

Short Block Sitting In PERELANDRA’s Main Salon

I did borrow Mark’s pressure washer, and brought it over to DREAM AWAY. I washed down the topsides and it really got rid of a lot of dirt. Very pleased.

My new Evolution Rage III compound miter saw arrived, but did not have time to unpack it.

July 25, Thursday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Spent extra time working on email, scanning and updating the maintenance log

I then applied the third coat of varnish on teak pieces to cover the davit holes in aft cabin, the teak piece to cover the winch hole in the main cabin, and the teak electrical wire cover. I also applied the second coat of Watco teak oil finish to the boom gallows, and the second coat to the instrument cluster housing, and the bell holder.

July 24, Wednesday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Spent a couple of extra hours working on getting caught up on email, and the maintenance log.

Went over to the Port’s storeroom and picked up the lawn mower, trimming shears and the wasp spray. Came back to the marina, and cut all of the grass, and trimmed around the trees, and along the edges of the grass. I then weeded all of the gardens.

I then took apart the Nicro day/night vent that had not been working. The vent is located in the overhead of the head. I removed the battery, and the solar vent started working. I checked the battery and it was as dead as a rock! Now the vent works during the day. As soon as I can get a rechargeable “C” NiMH battery, I will have the day/night vent back.

Loaded the lawn equipment into the Black Beast, and took it back to the Port of Delcambre’s storage room. Then it was off to the shop, which is actually at the other end of the storage room building!

I then applied the second coat of varnish on teak pieces to cover the davit holes in aft cabin, the teak piece to cover the winch hole in the main cabin, and the teak electrical wire cover. I also applied the first coat of Watco teak oil finish to the boom gallows, and the second coat to the instrument cluster housing, and the bell holder.

July 23, Tuesday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Drove into New Iberia to get my new TWIC card. That was fun! Could not schedule an appointment because the scheduling system had been down for seven days! Had to go in on a first come first serve basis. I was fourth in line, and it took 2.5 hours. The Internet connection kept going up and down, but I was finally successful. I now have the TWIC card for three more years.

Did some shopping, and then back to DREAM AWAY to catch up on email, scanning and the maintenance logs!

Went up the main mast to work on the Taco LED spreader light that I had installed on the starboard spreader this past July 14th. When I initially installed the Taco LED spreader light, I did not use the shrink wrap butt connector. I wanted to see if the new Taco LED spreader light would give out as much light as the Hella Marine Halogen Deck Floodlight. I was pleasantly surprised, and vowed to replace the four 55 watt Hella Marine Halogen Deck Floodlights with four 6 watt Taco LED spreader light.

Since I wanted to keep the one Taco LED spreader light, I needed to replace the butt connectors with shrink wrap butt connectors. I also had to put a nut on a bolt to adjust the light. I did not have the correct metric nut the first time up the mast. I had purchased what I thought was the correct nut. When I got up the mast to the Taco LED spreader light, I then discovered I had the wrong nut, and broke one of the shrink wrap butt connectors, and I only had two! So the effort was pretty much wasted. I completely disconnected the Taco LED spreader light and brought it down with me when I came down the mast.

This way I can insure I have the proper nut, and the shrink wrap butt connectors will already be on.

July 22, Monday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went over to shop and did final sanding on boom gallows. All of the voids had been filled, so we were ready with the next step.

Sanded Boom Gallows

I hung up the boom gallows from the overhead. This was so I would have access to all four (six) sides of the boom gallows. I then mixed a batch of Smith’s penetrating epoxy, and applied it to the boom gallows.

Smith’s penetrating epoxy Applied To Boom Gallows

Took apart Sealand pump and removed the duck bill valves from the valve housings, and the pump itself. I then put all of the parts in a bucket of water to soak to try and get the build up of calcium removed. This will be a long dirty process!

Hopefully I will be getting into working on the main mast sail deck, which will require welding of aluminum. To help with the preparation, I decided to practice filling a hole in a piece of scrap aluminum. The effort worked out very well.

Practice Weld On Scrap Aluminum

I then went back to marina. The project for today was to clean all of the power pedestals on “C” dock. I had purchased a long handled brush for just this purpose. It would clean away spider nests and wasp nests, and my hands would not be very close to the activity! I got all of the pedestals cleaned, and there was no wasp nests!

I went back to the shop and applied the first coat of varnish on teak pieces to cover the davit holes in aft cabin, the teak piece to cover the winch hole in the main cabin, and the teak electrical wire cover.

Varnish Applied To Teak Pieces

After the varnish application, I applied the first coat of Watco teak oil finish to the instrument cluster housing, the bell holder, and a third coat on all of Troy’s wood.

Watco Teak Oil Finish Applied To Hanging Instrument Cluster

Watco Teak Oil Finish Applied To Troy’s Wood & Bell Holder

July 21, Sunday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went over to the shop. The epoxy I had left yesterday had set up nicely. I was able to sand down the boom gallows again. I discovered I had five new hole to fill with teak bungs, and still had a few voids to fill where I had filled the slots in the boom gallows

I mixed a pot of epoxy, and used it to put in the teak bungs. I then mixed a small amount of teak dust with the epoxy, and filled in the voids.

Bungs And Voids Filled With Epoxy

While the epoxy was sitting up, I sanded smooth the teak pieces to cover the aft cabin davit holes, the piece to cover the main cabin hole in the overhead, and the teak wire cover for the main cabin. I wiped them all down with a tack rag to remove excess dust. I then applied the “agent orange dye” to all four pieces of teak wood.

Agent Orange Dye applied to the Teak Wood Pieces

I then went to DREAM AWAY and participated in a port meeting concerning the Safe Harbor Initiative with one of the shrimpers.

Then I had to fix the toilet. It would not pump out into the holding tank. I was pretty sure I knew what the problem was, and as it turned out I was correct! The duck bill valves were covered in calcium deposits, and would not allow the pump to work as designed. I had a new pump ready to go with all of the valves and housings. Because of the location it still took about three hours to get the job completely done.

Now I have to take the removed pump apart and clean it out thoroughly, install new duck bill valves, and it will be ready to go again.

July 20, Saturday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went over to the shop, and removed the Formica from the first filled slot on the boom gallows. Overall, not too bad of a job. Will require some sanding, and some voids that will need a fill in of epoxy0.

First Slot In Boom Gallows, Formica And Clamps Just Removed

Went through the same drill as yesterday for the second and third slot in the boom gallows. Used the Formica and the clamps with lots of epoxy to fill the second slot. When it was filled, I put the boom gallows outside in the sun to get the epoxy kicked off.

Second Slot In Boom Gallows Filled

When the epoxy in the second slot had kicked off, I filled the third slot. Had to use some extra weight to keep everything in place.

Third Slot In Boom Gallows Filled

Went back to DREAM AWAY for lunch. When I came back I mixed up a batch of Smith’s penetrating epoxy. I applied it to the Instrument pod, the two teak covers for the aft davit holes, the teak cover for the main cabin hole and the teak wire cover for the main cabin.

Smith’s Penetrating Epoxy Applied to Teak Pieces

The epoxy had kicked off on the third slot in the boom gallows, so I was able to sand down all three filled slots in the boom gallows. As suspected, there were some voids that would need filling with an additional application of the epoxy mash mix.

Voids In Slots Of Boom Gallows

Slots one and two were pretty easy to fill in. I used masking tape to build dams, and the just poured in the mixed epoxy. The mixed epoxy was a mild mash mix. By that I mean I mixed in a small amount of teak sanding dust. This thickens the mixture, but also gets closer to the real color of the teak wood.

Slot three turned out to be a bit short, so I had to add some teak wood to it. The good news was I had to cut off a high piece on one of the other slots, so it fit in perfect.

Masking Tape Dam On Slot Two Of Boom Gallows

Showing Extra Weight On Third Slot With Added Teak Wood

While working on the boom gallows, I found two more holes that needed to be filled with teak bungs. This will be done tomorrow, after the epoxy has set up over night.

July 19, Friday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went to the shop to work on the Black Beast ignition problem. I will relate here the entries I put into the Chevy Truck Forum trying to get help with the problem.

I have a 1996 Suburban diesel that will not start. When I turn the key to the run position, all is well, when I turn the key to the start position, nothing happens. I have done a bunch of troubleshooting, and have narrowed down the problem to the gear mechanism between the cylinder and keys and the ignition switch.

If I remove the ignition switch from the steering column, and turn the ignition switch with a flat blade screw driver, it goes to the run position, then the start position, and the engine starts normally. When I turn the key in the cylinder, the gear that operates the ignition switch turns, and does not seem to have a problem. When I put the ignition switch into the gear mechanism, and turn the key, the engine will not start.

Has any one seen this problem and have a fix for it? What is the gear mechanism that connects the ignition switch to the cylinder and keys called? I can not find the part name on any parts list.

Not sure of the how or why, but the problem has been repaired. Hopefully the fix is long lasting, but I am not sure. I swapped in a new ignition switch and I got the same symptoms as I described in the original problem. Put back in the original ignition switch, and the same problem was there, so it seemed like the problem was not the ignition switch assembly.

We took the original ignition out of the vehicle, as I wanted to ohm out some of the connections. I took the wrong side of the switch apart, and six little springs went flying! I recovered four of the springs, but could not find the other two. I took two ball point pens apart, and used the springs out of the pens in the ignition switch, and put the switch back together.

We put the ignition switch back in the vehicle, and it worked! Tried starting the vehicle several times, and it always worked. We put the steering column and all of the sundry parts back together, and it still works.

That was yesterday, and I am still not having a problem. Not sure why the new ignition switch would not work, and not really sure why messing with the springs in the original ignition switch fixed the problem. Hope this information helps someone else!

That finishes the entries I put in the Chevy Truck Forum. Just a note here, I am actually writing this in the middle of August, and still no problem with the igintion switch!!

Put the lawn mower in the Black Beast, and went back to North Pier Marina. Kitty left to do errands and laundry in the Black Beast. I finished cutting the grass and the weeding of the gardens. When that project was complete, I took the mower back to the Port of Delcambre’s storage room, then went to my shop.

I cut the pieces of teak wood I am going to use as the fill-in for the rectangular cut-outs in the boom gallows. These pieces of wood are left over from the teak deck that was removed many years ago. I clamped pieces of waxed Formica on either side of the cut in the boom gallows. I also did a dry fit of the teak wood pieces in the cut out. I labeled each piece at to position and top and or bottom.

Formica And Clamps On Boom Gallows

I mixed up a pot of epoxy and started putting the pieces of teak wood into the cutout in the boom gallows.

Cut Pieces Of teak And Pot Of Mixed Epoxy

Initially I poured some of the mixed epoxy into the cutout in the boom gallows. I wanted to make sure I had plenty of epoxy on all sides of the pieces of teak.

Epoxy In Boom Gallows Cutout & First Piece Of Cut Teak Wood

Then it was just a process of putting epoxy all over each piece of cut teak wood, and inserting the piece into the cutout in the boom gallows. When all of the cut pieces of teak wood had been inserted, I put another clamp on the outside of the Formica to make sure it was a good tight fit.

Insertion Complete, Waiting For Epoxy To Kick Off

While the epoxy was kicking off, I cut out the second slot in the boom gallows, and also cut the pieces of teak wood to be used as the filler.

Boom Gallows Marked For Rectangular Cutout

Cut Made On Boom Gallows

Cut Teak Wood Pieces In Rectangular Cutout

Long day finished, went back to DREAM AWAY for a shower and supper.

July 18, Thursday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went over to the shop and continued work on the boom gallows. As I figured, I found my jar of screw starters and bung cutters where I had put them last! I did not have enough ⅜” teak bungs, so I had to cut about 50 of them. Having a drill press and some scrap teak really helped this process.

Cutting Teak Bungs

Mixed up a pot of epoxy, and epoxied all of the bungs needed on one side of the boom gallows. I set the boom gallows out in the sun. When the epoxy had kicked off, I brought the boom gallows back into the shop, mixed another pot of epoxy, and epoxied the bungs into the other side of the boom gallows. The boom gallows went back out to the sun to kick off the epoxy.

While that batch of epoxy was kicking off, I sanded and scraped off all of the old Cetol on the instrument cluster. Had to be down to bare wood.

Went back over to the North Pier Marina, as it was that time of the week to cut the grass and do some additional weeding of the gardens. I cut grass until the rains came. Will finish that project tomorrow.

Went back over to the shop to continue work on the boom gallows. Right after I had installed the hard bimini, I realized I would have to fill in the slots for the boom on the boom gallows.

Slots For The Boom On The Boom Gallows

I had cut out some pieces to fill in the slots, I have just never had the time to shape the pieces and fill in the slots in the boom gallows. The time had come! I started in on shaping the pieces to fill the slots.

Teak Piece For Slot In Boom Gallows

I worked at the teak pieces, and it was going to be a chore to try and get the pieces to fit the curved, angled slot in the boom gallows. I decided to go at it another way. I did not have any teak as thick as the boom gallows, but I could cut out four or five pieces to a better shape and epoxy them into the slots. I worked on that for some time.

Pieces Cut To Fill Slots In Boom Gallows

Pretty soon I came to realize that I am a fair carpenter, but I was never going to get the pieces shaped properly. I came up with plan “C”. This plan is to cut rectangular slots in the boom gallows, completely removing the curved, angled slots. With a rectangular hole to fill, I would be able to cut the necessary pieces, epoxy them into place, and the boom gallows would look very good.

This new plan would be started on the morrow!

July 17, Wednesday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went over to the shop and cut out the teak piece for the main cabin overhead, and the two pieces for the aft cabin davit holes.

One Of The Aft Cabin Davit Holes

Went back to DREAM AWAY, and completed removal of the boom gallows. Loaded the boom gallows into the Black Beast.

Boom Gallows Removed

We then went off to New Iberia to attend a Port of Delcambre luncheon about safe harbor in Vermillion and Iberia Parish.

Came back to Delcambre, got Mark and we headed off to the Dugas Engine Services shop in New Iberia to pick up Mark’s engine block, crankshaft, and my power head (yea).

Came back to Delcambre, unloaded the crankshaft, the engine block, and my power head.

I got back into work on the boom gallows. I drilled out all of the “extra” holes in the boom gallows where screws used to be, but were no longer. I drilled them out for teak bungs to be inserted. I still have not been able to locate my jar of screw starters and bung cutters

Had to leave early, to prepare for and attend a pot luck supper for and by the Delcambre Seafood and Farmers Market. It was put together by all of the vendors, just to have a social.

July 16, Tuesday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Had breakfast and then started striping the boom gallows. The boom gallows needed some work in preparation for installing the hard dodger. There were also three indentations in the boom gallows in which the main boom could drop. These were not needed anymore because the hard bimini interfered with the indentations. I wanted to fill in these indentations so the boom would not fall into them and damage the solar panels I plan to install on top of the hard bimini, in the future.

I removed the external speakers, the instrument cluster, and all of the associated wiring. I removed the track and supports for the soft dodger. I also removed the bolts attaching the hard bimini to the boom gallows. Without the boom gallows in place the hard bimini would just lean against the boom gallows supports.

Boom Gallows Before Removal

When I had all of the removed parts from the boom gallows, I put all of the pieces in the Black Beast. Kitty then drove me over to the shop, I unloaded all the boom gallows parts and started in to work on them.

The plan is to sand down all of the parts, including the boom gallows, soak them with Smith’s penetrating epoxy, then apply at least three coats of Watco teak oil finish. The first pieces to work on was the instrument cluster. This had to be scraped and sanded to bare wood.

Working On The Instrument Cluster

Went to lunch, and then back to the shop. Started in on the instrument cluster, and Kitty called and said there was a problem with the Black Beast. The ignition switch would not start the engine!

Was able to get the Black Beast started, then drove it over to the shop. Spent the remainder of the day working on that problem. At the end of the day, 1800, we (Mark and I, mostly Mark) had the ignition switch off of the steering column, and with a flat blade screw driver, were able to start the Black Beast at any time.

July 15, Monday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Had breakfast, and went over to the shop and started in on the teak pieces I had epoxied yesterday. I already had templates made for the pieces I needed to cut out, so I marked off the templates on the teak. These two pieces are going to be used to cover the holes cut in the aft cabin bulkhead to install the backing plates for the dinghy davits.

Templates On Fabricated Teak Piece

Cut Marks On Fabricated Teak Piece

I realized I had enough wood remaining in my fabricated teak piece, I could cut out another piece to cover a hole in the overhead of the main cabin, which I did.

Hole In Main Cabin Overhead

I am working on fabricating a deck from the main mast to the cabin top as an area to work on the main sail. I will be referring to this project as the main mast sail deck. I have some aluminum pieces at the shop I am going to use as the primary support at the main mast. These pieces had to be cut and modified. I used my chop saw to cut the piece, and then sanded it down smooth. In the future I will weld up the present holes in the piece.

Piece After Cut In Chop Saw

Piece Sanded Smooth

Went back to the boat, and pretty much spent the remainder of the day installing the new Pepwave Surf SOHO 3G/4G Router w/ WiFi as WAN. The actual Pepwave Router was not too much trouble, but the cable that had to run from the Hyperlink 1 watt WiFi amplifier, to the Pepwave Router was a lot of fun! The “why” of making this change is pretty well explained In the Maintenance Log entry of May 27, 2013.

Running Cable In Garage

Running Cable Past The EnGenius EOC1650 Bridge

Using Ziptape Wire Markers On Cable

Running Cable Past WiFi Power Supply

Pepwave Router Installed On Mid-Cabin Electronics Shelf

July 14, Sunday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went over to shop and removed the compressor from the air conditioner tray. When that was removed I finished cleaning all the junk and rust out of the tray. The tray is ready to send off to Stacy.

Finally got the epoxy pumps for my epoxy, so I was able to finally mix some up! I did mix a batch and epoxied a piece of teak to the piece I had made to cover the holes I had to cut for the davit backing plates. I had made the teak piece some time ago, but it was not wide enough.

Epoxying Teak Piece’s Together

I also added a couple of small pieces of teak to a teak wire cover I am using to cover electrical wires in the main cabin.

Teak Electrical Cover Being Added To

I used my chop saw and started doing some experiments with putting a curve in the stainless steel tubing. I am pretty sure it will work, so I might use it for the fabrication of the stern ladder. The theory is to cut out a portion of the metal at a thirty degree angle, then gently bend it back together, and weld it.

Experimental Cut Square Tubing

I had finally received the gun cleaning kit I ordered. I have not cleaned the line launcher since our trip to Atlanta at the first of just, so it was due. I got the line launcher cleaned, oiled down, and all put back into it’s case.

Line Launcher With Cleaning Gear

Went back to DREAM AWAY, and had breakfast, then up the main mast.

The wind instrument had quit working. I have a spare piece of cable and wind vane, so I had connected them directly to the wind instrument, and it worked great. I then disconnected the cable that came down from the top of the main mast at the junction box and connected the spare wind vane cable at the junction box. The wind instrument worked just fine.

Now it was time to take the wind vane up the main mast and install it. I took it up to the top of the mast and removed the old vane and installed the spare. When we tried the wind instrument, it worked great. So now I had to get the wind vane repaired.

Captain Jim At The Top Of The Main Mast

While I was up the mast, I replaced the starboard main spreader light with Taco LED spreader light. It is a big difference in power consumed. The Taco LED spreader light uses 6 watts, and the Hella Marine Halogen Deck Floodlight uses 55 watts. The issue is the Hella Marine Halogen Deck Floodlight really lights up the deck at night. I purchased one of the Taco LED spreader lights to see if it would compare with the Hella Marine Halogen Deck Floodlight.

I did a quick installation, and then back down to the deck. I waited until the night, and was pleasantly surprised with the amount of light put out by the Taco LED spreader light. Now I will have to purchase three more of the Taco LED spreader lights.

I just might use one of the Hella Marine Halogen Deck Floodlights back on the dinghy davits to light the area when getting into and out of the tender at night, and also as a security device.

July 13, Saturday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

took off tender hold down lines and started wash process; removed soft dodger; measures bracket for main mast base grating; helped Joel with air conditioner.

Went to the shop first this in the morning and started cleaning up the parts on the spare Yamaha Outboard. Hopefully I will be getting back the repaired power head and will be able to reassemble the spare engine.

Upper Casing Getting Cleaned Up

I continued working on the tray for the failed air conditioner. My son, Stacy, has a friend who can fabricate the tray out of stainless steel, and he offered to get it done for my spare Cruisair Air Conditioner. What I need to do is strip all of the parts out of the tray so it can be sent off to Stacy’s friend. Once all of the parts are out of the tray, then the tray itself will have to be cleaned out.

Evaporator Removed From Tray

Air Conditioner Tray With Compressor

Went back over to DREAM AWAY for breakfast, and afterwards, I installed the washed and clean sheet nets in the cockpit.

Aft Cockpit Without The Nets

Aft Cockpit With The Nets

The new J-Bolts I had ordered came in so I am able to bolt down the fiberglass gratings I had cut for the bow pulpit. First I had to clean the bow pulpit deck and seat area in the bow pulpit before I installed the gratings.

Bow Pulpit Deck Before Cleaning

Bow Pulpit Seat Before Cleaning

Bow Pulpit Deck After Cleaning

Bow Pulpit Seat After Cleaning

Grating Installed On Bow Pulpit Deck

Grating Installed On Bow Pulpit Seat

J-Bolt And Grating Detail

I took off the tender hold down lines off of the davits to clean them up. They had been unused for some time, and were getting green. It was time to start washing lines on DREAM AWAY, and these were it. The plan was to soak them in a bucket with a mild bleach and soap solution, for a couple of days.

Lines Getting Ready For The Bucket

Last item for today is to remove the soft dodger. As you can see from the pictures, it needs replaced, and we are going to replace it with a hard dodger. The boom gallows needs work, so the soft dodger has to be removed for that project also.

Soft Dodger Before Removal

Soft Dodger Removed

I then helped our neighbor Joel with his air conditioner. We were able to remove the AC unit from his boat, and really get a good look at the burnt capacitor. We were able to get the capacitor removed, so he could use it to go get another one at an electric supply store in New Iberia this coming Monday.

July 12, Friday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Started off the day by cleaning out the main strainer for the manifold (Sea Chest), and the manifold (Sea Chest). Also cleaned out the strainers for the ice maker cooling pump, the refrigeration cooling pump and the forward air conditioner cooling pump. During this cleaning process, I also cleaned out the hoses for all of the cooling pumps. I clean out each hose by sending water through each hose with water from the dock!

Went out to pier C and checked the electrical issues on the 29/30 pedestal.

Finished up work on Hollis’s boat. Was able to finally get the diesel leak on the generator repaired. I also changed the oil and the oil filter and fuel filter on his generator. Hollis was a happy camper.

Helped Joel with his air conditioner problem. Could not resolve problem, we need to remove the unit to get a better view of the electrical parts at the back of the unit.

July 11, Thursday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Did not go over to the shop first thing, stayed on DREAM AWAY and worked on getting caught up on email, financial issues, and updating the Maintenance Log and web page.

Went to a safe harbor meeting for the Port of Delcambre in New Iberia. Well worth the effort!

Came back from the meeting and purchased docking lines at Touchard’s. Returned to Marina and installed the lines on the designated boat. Cleaned all of the power pedestals on pier B, and weeded the south garden at North Pier Marina.

I then went over to the shop and worked on cleaning up the parts for the spare Yamaha outboard engine. I also worked on smoothing out the rough places on the new grate in the seat on the bow pulpit.

Grate To Replace Seat On Bow Pulpit

July 10, Wednesday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Did not go over to the shop first thing, stayed on DREAM AWAY and worked on getting caught up on email, financial issues, and updating the Maintenance Log and web page.

Helped Mark with his engine. We loaded the stripped block and the crankshaft into the Black Beast. We also put in my spare Yamaha powerhead, and drove into New Iberia to the machine shop. We dropped off both parts. They are going to drill out my powerhead and put helicoils in it, and bore out Mark’s block.

When we returned, I got the lawn mower and cut all of the grass at the Marina. Next I helped Hollis with his boat, but when we went to the Onan dealer, they did not have the correct part, so we ordered what we hope will be the correct part.

July 9, Tuesday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Did not go over to the shop first thing, stayed on DREAM AWAY and worked on getting caught up on email, financial issues, and updating the Maintenance Log and web page.

Helped Mark work on his engine, helped Hollis work on his boat, and worked on the Marina gardens! No work done on DREAM AWAY.

July 8, Monday, 2013

About mid-morning, Jimmy and Barbara left to go back home in Houston. Kitty and Connie, off of IMPETUOUS, drove over to Orange, Texas, so Kitty could get her driving license.

I stayed in Delcambre and worked on Hollis‘s boat at North Pier Marina with the owner for the remainder of the day. He had some engine issues, leak issues and air conditioning that he needed some help with.

We got the main engine issue solved, still working on the diesel leak on the generator.

Kitty did get her driving license, and was back in Delcambre by 1900. Long wait for the license!

July 6 and July 7, Friday & Saturday, 2013

Did not do any work on DREAM AWAY during this time. We just kicked back and enjoyed our friends while they were here. I had a couple of small projects planned with Jimmy’s help, but the weather was most uncooperative, so did not get them done.

July 5, Friday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Got called out to help Mark unload the new engine he had purchased to replace the blown one in his trawler. We moved the old block out of my shop and then put the new engine in the shop on a pallet. Now between the new combine engine and the blown marine engine, he will be able to build a pretty good running marine engine.

New Engine In Shop

New Engine In Shop

We then got a call to come over to the marina to help another boat back into the marina. This boat had gone out for a couple of days, but had lost an engine. Once we got the boat in its slip and settled, a dive under the boat found a crab trap line wrapped around the shaft.

Since Wayne, off of IMPETUOUS, was already in his SCUBA gear, I asked him to check the prop on DREAM AWAY. Not good, he confirmed my suspicions. The prop is nothing but a ball of barnacles. The prop and shaft will have to be scrapped before we go out sailing. Another project to add to the list!!

Went back to the shop and cut out the grating for the seat in the bow pulpit. I had the old teak seat to use as a pattern, so I probably got the new grating pretty close.

Grating Cutout & Old Teak Seat On Workbench

Late in the afternoon, our good friends from Houston, Jimmy and Barbara drove in from Houston, so we kicked back and enjoyed their visit.

July 4, Thursday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Did not go over to the shop this morning. Stayed on the computer and worked on updating the June Maintenance Log. Did some work for the port moving a boat, and then using my lines to moor it in it’s slip.

Worked most of the day getting ready for our Independence day cookout. Had a great cook out with Kittie and Mark from the marina, and new friends Wayne and Connie off of a transient boat staying in the marina for a few days, and Miss Glo. We all ate more than we should, but we cleaned up, and then drove over to Otto Herbert Lumber. We set up our folding chairs and watched the fireworks display put on by the town of Erath. It was a great day, and we were all happy to lay heads on pillows.

July 3, Wednesday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Went over to the shop and picked up the finished Panduit wire duct covers. Then I went to the Port of Delcambre’s storage room and pick up the lawn mower, after topping off the gas tank. I came back to the marina and mowed all of the grass. It was a much easier job than last week because the grass was not near as high. Only took about 1.5 hours! When I finished the grass, I loaded the mower back into the Black Beast and took the mower back to the storage room.

When I got back to the marina I took the two Panduit wire duct covers to the boat. After breakfast I installed the two pieces in the aft cabin. Not an easy task as all of the books on the starboard and port side had to be removed before the Panduit wire duct cover could be installed. I also had a little help from Jordan.

Panduit Wire Duct Cover Before Installation

Panduit Race Track With Wires Exposed And Helper

Wires Exposed

Panduit Wire Duct Cover After Installation

Next task was to dress ship using all of normal flags, and the International Code Flags. This was an easier task than normal. When I dressed ship for National Marina Day this past june, I left all of the flags together and just folded them up as they were. I got all of the flags up, and even put up our ships burgee.

DREAM AWAY Burgee

DREAM AWAY Dressed Ship

When I finished with the flags, I walked over to the shop and picked up the shelf I had been working on to install in the storage area under the galley stove. I also picked up the necessary tools for the installation, and walked back to DREAM AWAY.

The installation of the shelf was not a big issue, the problem is the space to work in! Too large a person working in too small a space. After much slippin’ and perhaps a four letter word or two, the shelf was installed. Now when we remove a pan or anything from the front of the storage area, all the items in the back will not slide forward.

The bad news is, because the shelf has new white paint on it, it is plain to see how much the other white paint in the storage area has faded. Another project for the future!

Front Of Storage Area Under Propane Stove

Shelf Not Installed

Shelf Installed

Storage Area With all Items Back In Area, New Shelf With Pans

Last item for the day was to remove the seat that is on the bow pulpit of DREAM AWAY. I am going to use the same fiberglass grating on the seat that I installed in the anchor area of the bow pulpit.

As you can see from the picture, the teak wood is in desperate need of maintenance, so I am working to get rid of maintenance issues. Replacing the teak with fiberglass grating will accomplish that task nicely.

Fiberglass Grating On Anchor Area Of Bow Pulpit

Teak Seat That Was Removed From Bow Pulpit

We got showered up, and had dinner on Wayne and Connie’s boat, the drove over to Erath, Louisiana, to see the Fourth of July festival and to listen good cajun and zydeco music. The featured band was Geno Delafose & French Rockin’ Boogie. It was a great time.

July 2, Tuesday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee. Spending extra time working on the June Maintenance Log to put up on the web page.

Went into New Iberia and had the new air conditioning compressor installed on the Black Beast. When that was finished, I came back to DREAM AWAY and had lunch.

After lunch I set up to test my freshwater pumps. One had quit working, and the was an easy fix. The micro switch that allows the pump to turn on was dirty. I sprayed some corrosion block on the switch and actuated it several times and that cleared the problem.

Now I got out two pieces of ½” hose and attached to the pump. I then got a bucket and filled it with water and brought it down into the garage. I connected my jumper cables to the battery and verified pump operation. The pump leaked, so I took it apart and cleaned up all of the mating surfaces. I put the pump back together and used never-seize on the bolts.

Freshwater Pump Being Tested In The Garage

The pump worked perfectly this time! I connected the hoses to the second pump and verified it’s operation. Both pumps worked as advertised, and I put them back into the spares locker.

I also helped a fellow boater solve his air conditioning problem. He had cleaned the strainer for the air conditioner, and now he was not getting water through the system. I initially thought the problem was the pump needed primed, but it turned out to be simple. He had forgot to open up his seacock after cleaning the strainer! We open the seacock, and the air conditioner worked just fine.

We then welcomed back another transient into the marina. They were very happy to be back with us.

July 1, Monday, 2013

Started off the morning with my normal ritual of getting on the Internet, answering email, checking the weather, while making a pot of coffee.

Day started off with me accompanying Kitty to the Iberia Medical Center for a CAT scan, that did not work out as planned. On the way home I noticed the air conditioning compressor on the Black Beast was not coming on.

I knew this was a problem that would come up because the noise the compressor was making when I had to change the harmonic dampener earlier in the year. So off I go to Chabill’s Tire Service to get the compressor replaced. Chabill’s Tire Service is where I originally had all of the air conditioning work done. I had a two year warranty on the compressor, and one year on the labor.

Lots of back and forth, that I will not go into, but the new compressor is on order, and I have to go back tomorrow at 1000 to have the work done! Then I went back to DREAM AWAY, and finally had breakfast and lunch, 1400!

Went over to the shop and sanded down the shelf I am building for the area under the propane stove in the galley. I also sanded the white area of the V-berth insert, and the Panduit wire duct covers.

Shelf Sanded And Ready For Paint

V-Berth Insert Sanded And Ready For Paint

I did the deed with the tack rag, and applied the fourth coat of varnish to the Panduit wire duct covers.

Varnish Applied To Panduit Wire Duct Covers

I then mixed up a batch of the two part paint I have left over from Guatemala, and painted the top of the galley shelf, the shelf supports and the top of the V-Berth insert.

Painted Shelf And Supports

Painted V-Berth Insert

I left the shop and went back to the marina, and performed my daily gardening activity. This means I pulled weeds out of the marina landscaping for about 30 minutes. This is an ongoing part of my part time job as the Marina Maintenance man!